Nose to the grindstone

5251

Boeing 747-312 VH-INH
Sydney (Kingsford-Smith) Airport,
12:22 pm, 19 October 1994

Every accident, no matter how minor, is a failure of the organisation.
– Jerome F Lederer 1902–2004

Nobody was hurt but this crash exposed fundamental organisational flaws and skated close to the cliff edge between black comedy and tragedy.

When the Boeing 747 reached 31,000 feet, Kate McAuley thought the worst was over. A late connection meant she had nearly missed the flight that was now taking her to a new life in a new city, where a new husband was waiting for her. As Ansett flight 881 passed the approximate latitude of Coolangatta, 3 decades ago, heading north, she turned her thoughts to the future. Then came an interruption.

‘We were near Brisbane, when the pilot said in English that oil was leaking from an engine and we had to turn around – we couldn’t land in Brisbane because the plane was too heavy,’ McAuley says now, from the US.

‘I was angry because I wanted to start my new adventure. I was, ‘Like, whatever!’ I was only a teenager.’

For the next hour she was alone in her irritation. ‘I was surrounded by Japanese honeymooners – everyone happily taking videos and photographs.’ McAuley also watched the ‘beautiful, surreal horizontal waterfall’ of fuel being dumped from the Boeing 747’s wings.

‘About 15 minutes before we came into land, they translated the pilot’s announcement into Japanese and the cabin crew were rushing through the cabin making sure everyone had their seat belts on.’

Flight 881 returned to Sydney on a grey wet spring day on 3 engines and began a standard instrument approach from the West Pymble locator. The windscreen wipers were dancing as they emerged from cloud at 500 feet with Sydney’s then-single runway 16 ahead of them.

‘After we touched down, it felt like we were nose-high,’ McAuley remembers. ‘Then … the reports said the pilot gently laid the nose on the tarmac. That didn’t happen – it was very loud, a lot of careening and very bumpy, grinding noises and sliding left to right. It was not a pleasant experience.’

image: BASI

What happened

The aircraft had landed with its nose gear retracted. It was the first, and so far, the only time, a Boeing 747 has done this. Other 747 nose gear collapses have involved human error in maintenance, the wheels hitting approach lights or objects near the runway after a runway excursion.

On the way back to Sydney, the crew had briefed for the landing, including the possibility that gear extension would be slower. The captain was pilot monitoring, the first officer was pilot flying, and the flight engineer was intermittently busy replying to airline management by radio to arrange accommodation and onward flights for the passengers.

The gear had been lowered at 2,000 feet. The first sign of trouble was 50 seconds later when the flap lever was moved from 20 degrees to 25. The landing gear warning horn sounded which the captain rationalised as the gear being in transit. He moved the lever back to 20 degrees, thinking this would direct more hydraulic pressure to the gear. He asked the engineer to check the gear panel, to which the engineer replied, ‘Four greens.’ The captain later said he may have heard this as, ‘All greens.’ The crew were not using headsets.

At 500 feet, the captain asked the flight engineer if all green lights were on for both primary and secondary indicating systems. The flight engineer responded that they were. The captain said he was perplexed by the still-illuminated red gear warning light on the centre instrument panel. Seven seconds later, the flight engineer said the flaps were still running. The captain indicated he was still concerned about the landing gear warning horn, which indeed sounded until touchdown.

As the Boeing crossed the Alexandra Canal on the last stages of its descent, it was flying at 186 knots, a considerable 26 knots faster than the calculated reference speed for final approach (Vref). Observers saw ribbons of condensation trailing from its wings. As the crew were about to lower the nose, they heard from the tower that the nose gear had not deployed. There was a momentary consideration of a three-engine go-around, but this was quickly rejected and the crew let the nose settle to the runway.

As the crew were about to lower the nose, they heard from the tower that the nose gear had not deployed.

From the report

An unexplained reduction in air-driven hydraulic pump output caused slower than expected operation of the number one hydraulic system. The system may still have been capable of extending all the landing gear, given adequate time. However, the aircraft landed before the system could complete the landing gear extension. The flight crew had the opportunity to recognise and correct the landing gear problem prior to landing. The pilot in command attempted to determine the actual landing gear situation from the flight engineer. Although the flight engineer’s panel indicated the nose gear was not down and locked, the flight engineer did not recognise this and subsequent communication and coordination between the flight crew failed to detect this error.

Although the flight engineer’s panel indicated the nose gear was not down and locked, the flight engineer did not recognise this.

Why it happened: the technical picture

The Bureau of Air Safety Investigation (BASI), precursor of today’s Australian Transport Safety Bureau, investigated the crash. The bureau found that the oil loss was caused by the failure of a threaded insert used to retain the engine angle gearbox housing cover. A service bulletin for this precise issue, SB JT9D-7R4-72-410, had existed since 1990 but was not mandatory and neither Ansett nor the aircraft’s previous operator, Singapore Airlines, had actioned it.

The landing gear was normally driven by the hydraulic pump powered by the No 1 engine, as the flight crew knew. But, as one of the 747’s many design redundancies, a second identical pump was driven by a common manifold that took bleed air from all 4 engines. In the auto setting selected as part of the flight engineer’s checklist, this pump acted to maintain hydraulic pressure at or near 3,000 psi.

There had been 3 maintenance log entries in 4 weeks reporting problems with this number one air-driven hydraulic pump system, the most recent being 9 days before the crash. However, engineers were unable to replicate the fault. When the aircraft was test flown after the crash, the pump worked perfectly.

What allowed it to happen? The big picture

One false move and we could have a farce on our hands. – Tom Stoppard

The crash occurred at the perfect time in production schedules for newspapers and TV that dominated media in those days and Ansett suddenly had abundant if unwanted publicity for its new international route. The airline had begun international flights to Bali in 1993 and on 30 March 1994, its directors decided to expand operations to the new Kansai airport in Osaka, Japan. The first service was to be on the airport’s opening day, 4 September 1994. A project team took on the task’s many elements, but its manager left in July 1994.

Flight crew training quickly emerged as a problem area. An initial arrangement for Qantas to conduct line (operational flight) training was scuppered by industrial action. Two ex-Singapore Airlines’ Boeing 747s arrived in May, only for Qantas to withdraw from ground and simulator training, which it had expected would be linked to a lease of its Boeing 747s. The date for crew training commencement was pushed back by a month.

Contract crews were hired for a four-month term from September 1994 to January 1995. On 9 June after high-level discussions between Qantas and Ansett, simulator and ground training at Qantas were restored. At once there was a divergence of philosophies. Qantas recommended its training course, but Ansett preferred the Singapore Airlines version of the Boeing operations manual, amended to reflect Ansett practices. One such divergence was the role of the flight engineer. It was regarded as a technical specialist by Ansett but as an integral member of the crew by Qantas, whose flight engineers had specific duties of checking and monitoring, and a general role as a flight deck resource.

Training was intense and conducted at unusual hours when the simulators were available. The courses were confused and disorganised, with attendees reporting, ‘Unsigned, unattributed sheets of paper containing amendments to operational procedures were distributed to trainees during the night.’ One pilot reported knowing 3 different checklists, based on Qantas, Boeing/Singapore Airlines and Ansett procedures. Three pilots on the first course did not complete the program and overall final check failures were high: 6 of the 13 pilots and 2 of the 6 engineers failed their first simulator final check. The Qantas simulator had Rolls-Royce engines while the Ansett aircraft had Pratt & Whitney engines, requiring supplementary training, and unlearning of some simulator drills.

On 19 October, this roulette wheel of shortcomings and shortcuts by operator, regulator and crew came up short.

Nonetheless, Ansett’s inaugural Boeing 747 ‘spaceship’ flight to Kansai took off on 4 September and landed without incident.

The experience of the crew on the day of the incident was unevenly distributed and they had no common set of standard operating procedures between them.

  • The contracted captain was highly experienced, with 21,500 hours, including 7,500 on type, recently retired from Cathay Pacific Airways.
  • The first officer had 7,100 hours including 80 on type, all of it training. However, an illness meant the first officer had not undergone a line check before the flight.
  • The flight engineer, one of 2 who had failed their final simulator check, was on their first revenue flight on type.

BASI listed other significant local factors which influenced the performance of the flight crew:

  • cockpit noise levels – high
  • subtle pressures – management suggested the crew ‘turn around’ to fly the replacement flight in another aircraft.
  • flight engineer’s lack of preparedness for the task
  • flight engineer’s panel skills
  • task overload
  • layout of the flight engineer’s panel – there was no grouping of the 5 gear lights
  • crew resource management – was not required by the regulator at the time
  • stabilised approach procedures – were not followed.

Oversight by the then regulator, the Civil Aviation Authority, had been flawed. Line training oversight was managed from the Sydney office while Boeing 747 introduction was managed from Melbourne. And the authority ignored concerns raised by its own specialist 747 pilot.

On 19 October, this roulette wheel of shortcomings and shortcuts by operator, regulator and crew came up short. Another way to think of it would be as the holes inevitably lining up in a series of notably porous Swiss cheese slices.

Postscript: the next day

After the longest 15 minutes of her life, McAuley was evacuated, anticlimactically, via stairs and bus. She was given a cup of tea as disaster victim support and called her mother on a huge, heavy device known as a mobile phone.

She naively thought she might have to pay for the minibar in the hotel Ansett booked for her. The next day, when asked if she wanted to fly again, she surprised the staff by saying ‘Sure!’ – and was allocated the same seat on another 747.

The seat came with a free and unsettling serve of déjà vu. ‘Once we got past Brisbane, I thought ‘OK, it’s really happening – I’m on my way’.’

3 COMMENTS

  1. What didn’t get enough focus was the crew decision to ignore BN as a divert which was CAVOK and return to SY which was serious IMC, a 3 engine missed approach due weather minima was a real possibility. I departed SY about 10 minutes prior to the landing and vis was close to 4000mt RA and 200-400ft cloud base. Was divert chosen for engineering and pax considerations over operational? If ldg at BN, Tower ATC would have seen the no gear at 5nm from touchdown.

  2. I had served as a captain of Boeing 747-400, 747-300, and 747-200 jumbo jets. I flew both passenger and cargo configurations, as a captain for the 747-400 and 747-200 aircraft.

    Crossing the north Pacific, I was a fairly senior First Officer flying a Boeing 747-200 Freighter, when I heard a clattering noise beneath my seat and a very brief illumination of the N0.2 GPS Antenna light, which I had pointed out to the Captain, a great guy and former USAF pilot, and a much older, “wheels up, heels up” Flight Engineer. We continued along, almost mid-Pacific, when the noise and indication happened again and I had instinctively reach for my Oxygen Mask, just as the “cabin dumped” -or, rapid decompression, which precipitated an immediate raid descent and 180° turn by the Captain, who did not yet have his mask on. I shouted to put his mask on and he handed over. We diverted to Tokyo. The Flight Engineer could have saved the situation and it would have been quicker and cheaper to continue to Anchorage, had he gone to Manual on the Outflow Valves and if the captain didn’t automatically make a descending U-turn, that I had to quickly program into the INS. This is how things can and do go wrong . . . especially when shock and panic prevails, there is no crew coordination, checklists are not followed (explicitly), lazy-minded crew or a crewmember well past their use-by date (and, it can happen for a crewmember who is 45 or 55 -it doesn’t have to be the domain of over 60s), and when the rest of the crew does not trust or doubts the guy in the Right Hand Seat -or even riding in the Jump Seat. Turns out it was a faulty Ground Safety Relay.

    As it relates to the Ansett Boeing 747-312 mishap . . . the biggest error was not building in time to get the aircraft fully configured and making that “Stabilised Approach” at the 1,000 ft AGL Gate. If something is not right, lingering doubts about a system malfunction being corrected, not fully configured and on-speed, anyone on the Flight Deck, should call “Go-Around”.

    What was the problem with this aircraft and flight? Not much, except the Nose Gear Door Actuator sometimes requiring a bit of extra pressure. The Flight Engineer and Captain not effectively communicating. The Flight Engineer not being 100% familiar with the Flight Engineer’s panel that lights up like a Christmas tree (maybe too much information for him to have absorbed under pressure). Qantas training. And, the aircraft not on a Stable Approach.

    When I attended Qantas Boeing 737NG training, contracted by an overseas airline, we got awful time slots in the Flight Simulator, that nobody else wanted. I had five different Instructors and not one could agree on procedures, handling, or even how to program the FMC. And, worse, the overseas airline’s S.O.P. was a work-in-progress, thus there was a blend of operational expectations that not even the Chief Pilot had a handle on. Often, he would say, it’s in the S.O.P., but not ours, in fact. So, I have survived in a very similar environment as the crew of the ill-fated Ansett Boeing 747-312 crew.

    Another issue is that airlines acquire unwanted aircraft from airlines around the world. Instruments, lights and switches can be different. Flight Crew Operating Manuals for a particular aircraft from the airline it was acquired can be different from the airline it is sold or leased to and different again from the training organisation. And, worse, if you have a very experienced Training Captain from a different but well respected airline -with the mindset “That’s the way we did it at ABC Airline” can put undue stress on a new operation with a new aircraft type and their crew. I had served as a contract Captain for decades. When faced with these scenarios, my survival instincts would kick in and rely on Boeing, doing everything by the book, following checklists, studying before every flight -and when the company b.s. and politics got too deep, I would pack my bags and find a new home. That was a better alternative than having an accident on my record.

    Lessons to be learned: Be 100% by the book, exercise the best CRM on the flight deck and never be afraid to speak up when something is not right, must be on a stabilsed approach: fully configured, on-speed, checklist complete, protect your pilot licence at all costs . . . and, when the company b.s. and politics is too deep quit.

  3. we have had some ex-airline pilots in our Aero club. (Qantas)
    They have always been interesting to listen to, and often give good information and a profession attitude at all times.

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